Message ID | 20180423115844.26281-1-sebastian.reichel@collabora.co.uk (mailing list archive) |
---|---|
State | Accepted |
Headers | show |
Hi, On Mon, Apr 23, 2018 at 01:58:44PM +0200, Sebastian Reichel wrote: > The current reset-gpio support triggers an interrupt storm on platforms > using the maxtouch with level based interrupt. The Motorola Droid 4, > which I used for some of the tests is not affected, since it uses a edge > based interrupt. > > This change avoids the interrupt storm by enabling the device while its > interrupt is disabled. Afterwards we wait 100ms. This is important for > two reasons: The device is unresponsive for some time (~22ms for > mxt224E) and the CHG (interrupt) line is not working properly for 100ms. > We don't need to wait for any following interrupts, since the following > mxt_initialize() checks for bootloader mode anyways. > > This fixes a boot issue on GE PPD (watchdog kills device due to > interrupt storm) and does not cause regression on Motorola Droid 4. > > Fixes: f657b00df22e ("Input: atmel_mxt_ts - add support for reset line") > Signed-off-by: Sebastian Reichel <sebastian.reichel@collabora.co.uk> > --- > Changes since PATCHv2: > * fix patch description > * use same timeout value for soft and gpio-reset > --- ping. -- Sebastian > drivers/input/touchscreen/atmel_mxt_ts.c | 18 +++++++----------- > 1 file changed, 7 insertions(+), 11 deletions(-) > > diff --git a/drivers/input/touchscreen/atmel_mxt_ts.c b/drivers/input/touchscreen/atmel_mxt_ts.c > index 5d9699fe1b55..f97fbb0af020 100644 > --- a/drivers/input/touchscreen/atmel_mxt_ts.c > +++ b/drivers/input/touchscreen/atmel_mxt_ts.c > @@ -194,6 +194,8 @@ enum t100_type { > > /* Delay times */ > #define MXT_BACKUP_TIME 50 /* msec */ > +#define MXT_RESET_GPIO_TIME 20 /* msec */ > +#define MXT_RESET_INVALID_CHG 100 /* msec */ > #define MXT_RESET_TIME 200 /* msec */ > #define MXT_RESET_TIMEOUT 3000 /* msec */ > #define MXT_CRC_TIMEOUT 1000 /* msec */ > @@ -1206,7 +1208,7 @@ static int mxt_soft_reset(struct mxt_data *data) > return ret; > > /* Ignore CHG line for 100ms after reset */ > - msleep(100); > + msleep(MXT_RESET_INVALID_CHG); > > mxt_acquire_irq(data); > > @@ -3167,20 +3169,14 @@ static int mxt_probe(struct i2c_client *client, const struct i2c_device_id *id) > return error; > } > > + disable_irq(client->irq); > + > if (data->reset_gpio) { > - data->in_bootloader = true; > - msleep(MXT_RESET_TIME); > - reinit_completion(&data->bl_completion); > + msleep(MXT_RESET_GPIO_TIME); > gpiod_set_value(data->reset_gpio, 1); > - error = mxt_wait_for_completion(data, &data->bl_completion, > - MXT_RESET_TIMEOUT); > - if (error) > - return error; > - data->in_bootloader = false; > + msleep(MXT_RESET_INVALID_CHG); > } > > - disable_irq(client->irq); > - > error = mxt_initialize(data); > if (error) > return error; > -- > 2.17.0 >
On Mon 2018-04-23 13:58:44, Sebastian Reichel wrote: > The current reset-gpio support triggers an interrupt storm on platforms > using the maxtouch with level based interrupt. The Motorola Droid 4, > which I used for some of the tests is not affected, since it uses a edge > based interrupt. > > This change avoids the interrupt storm by enabling the device while its > interrupt is disabled. Afterwards we wait 100ms. This is important for > two reasons: The device is unresponsive for some time (~22ms for > mxt224E) and the CHG (interrupt) line is not working properly for 100ms. > We don't need to wait for any following interrupts, since the following > mxt_initialize() checks for bootloader mode anyways. > > This fixes a boot issue on GE PPD (watchdog kills device due to > interrupt storm) and does not cause regression on Motorola Droid 4. Out of curiosity, what is "GE PPD"? > Fixes: f657b00df22e ("Input: atmel_mxt_ts - add support for reset line") > Signed-off-by: Sebastian Reichel <sebastian.reichel@collabora.co.uk> Reviewed-by: Pavel Machek <pavel@ucw.cz>
Hi, On Wed, May 09, 2018 at 04:25:45PM +0200, Pavel Machek wrote: > On Mon 2018-04-23 13:58:44, Sebastian Reichel wrote: > > The current reset-gpio support triggers an interrupt storm on platforms > > using the maxtouch with level based interrupt. The Motorola Droid 4, > > which I used for some of the tests is not affected, since it uses a edge > > based interrupt. > > > > This change avoids the interrupt storm by enabling the device while its > > interrupt is disabled. Afterwards we wait 100ms. This is important for > > two reasons: The device is unresponsive for some time (~22ms for > > mxt224E) and the CHG (interrupt) line is not working properly for 100ms. > > We don't need to wait for any following interrupts, since the following > > mxt_initialize() checks for bootloader mode anyways. > > > > This fixes a boot issue on GE PPD (watchdog kills device due to > > interrupt storm) and does not cause regression on Motorola Droid 4. > > Out of curiosity, what is "GE PPD"? PPD is a product from GE Healthcare to monitor vital biometric signals: arch/arm/boot/dts/imx53-ppd.dts > > Fixes: f657b00df22e ("Input: atmel_mxt_ts - add support for reset line") > > Signed-off-by: Sebastian Reichel <sebastian.reichel@collabora.co.uk> > > Reviewed-by: Pavel Machek <pavel@ucw.cz> Thanks, -- Sebastian
Hi Dmitry & Nick, What's the status of this patch? -- Sebastian On Mon, Apr 23, 2018 at 01:58:44PM +0200, Sebastian Reichel wrote: > The current reset-gpio support triggers an interrupt storm on platforms > using the maxtouch with level based interrupt. The Motorola Droid 4, > which I used for some of the tests is not affected, since it uses a edge > based interrupt. > > This change avoids the interrupt storm by enabling the device while its > interrupt is disabled. Afterwards we wait 100ms. This is important for > two reasons: The device is unresponsive for some time (~22ms for > mxt224E) and the CHG (interrupt) line is not working properly for 100ms. > We don't need to wait for any following interrupts, since the following > mxt_initialize() checks for bootloader mode anyways. > > This fixes a boot issue on GE PPD (watchdog kills device due to > interrupt storm) and does not cause regression on Motorola Droid 4. > > Fixes: f657b00df22e ("Input: atmel_mxt_ts - add support for reset line") > Signed-off-by: Sebastian Reichel <sebastian.reichel@collabora.co.uk> > --- > Changes since PATCHv2: > * fix patch description > * use same timeout value for soft and gpio-reset > --- > drivers/input/touchscreen/atmel_mxt_ts.c | 18 +++++++----------- > 1 file changed, 7 insertions(+), 11 deletions(-) > > diff --git a/drivers/input/touchscreen/atmel_mxt_ts.c b/drivers/input/touchscreen/atmel_mxt_ts.c > index 5d9699fe1b55..f97fbb0af020 100644 > --- a/drivers/input/touchscreen/atmel_mxt_ts.c > +++ b/drivers/input/touchscreen/atmel_mxt_ts.c > @@ -194,6 +194,8 @@ enum t100_type { > > /* Delay times */ > #define MXT_BACKUP_TIME 50 /* msec */ > +#define MXT_RESET_GPIO_TIME 20 /* msec */ > +#define MXT_RESET_INVALID_CHG 100 /* msec */ > #define MXT_RESET_TIME 200 /* msec */ > #define MXT_RESET_TIMEOUT 3000 /* msec */ > #define MXT_CRC_TIMEOUT 1000 /* msec */ > @@ -1206,7 +1208,7 @@ static int mxt_soft_reset(struct mxt_data *data) > return ret; > > /* Ignore CHG line for 100ms after reset */ > - msleep(100); > + msleep(MXT_RESET_INVALID_CHG); > > mxt_acquire_irq(data); > > @@ -3167,20 +3169,14 @@ static int mxt_probe(struct i2c_client *client, const struct i2c_device_id *id) > return error; > } > > + disable_irq(client->irq); > + > if (data->reset_gpio) { > - data->in_bootloader = true; > - msleep(MXT_RESET_TIME); > - reinit_completion(&data->bl_completion); > + msleep(MXT_RESET_GPIO_TIME); > gpiod_set_value(data->reset_gpio, 1); > - error = mxt_wait_for_completion(data, &data->bl_completion, > - MXT_RESET_TIMEOUT); > - if (error) > - return error; > - data->in_bootloader = false; > + msleep(MXT_RESET_INVALID_CHG); > } > > - disable_irq(client->irq); > - > error = mxt_initialize(data); > if (error) > return error; > -- > 2.17.0 >
On Mon, Apr 23, 2018 at 01:58:44PM +0200, Sebastian Reichel wrote: > The current reset-gpio support triggers an interrupt storm on platforms > using the maxtouch with level based interrupt. The Motorola Droid 4, > which I used for some of the tests is not affected, since it uses a edge > based interrupt. > > This change avoids the interrupt storm by enabling the device while its > interrupt is disabled. Afterwards we wait 100ms. This is important for > two reasons: The device is unresponsive for some time (~22ms for > mxt224E) and the CHG (interrupt) line is not working properly for 100ms. > We don't need to wait for any following interrupts, since the following > mxt_initialize() checks for bootloader mode anyways. > > This fixes a boot issue on GE PPD (watchdog kills device due to > interrupt storm) and does not cause regression on Motorola Droid 4. > > Fixes: f657b00df22e ("Input: atmel_mxt_ts - add support for reset line") > Signed-off-by: Sebastian Reichel <sebastian.reichel@collabora.co.uk> Applied, thank you. > --- > Changes since PATCHv2: > * fix patch description > * use same timeout value for soft and gpio-reset > --- > drivers/input/touchscreen/atmel_mxt_ts.c | 18 +++++++----------- > 1 file changed, 7 insertions(+), 11 deletions(-) > > diff --git a/drivers/input/touchscreen/atmel_mxt_ts.c b/drivers/input/touchscreen/atmel_mxt_ts.c > index 5d9699fe1b55..f97fbb0af020 100644 > --- a/drivers/input/touchscreen/atmel_mxt_ts.c > +++ b/drivers/input/touchscreen/atmel_mxt_ts.c > @@ -194,6 +194,8 @@ enum t100_type { > > /* Delay times */ > #define MXT_BACKUP_TIME 50 /* msec */ > +#define MXT_RESET_GPIO_TIME 20 /* msec */ > +#define MXT_RESET_INVALID_CHG 100 /* msec */ > #define MXT_RESET_TIME 200 /* msec */ > #define MXT_RESET_TIMEOUT 3000 /* msec */ > #define MXT_CRC_TIMEOUT 1000 /* msec */ > @@ -1206,7 +1208,7 @@ static int mxt_soft_reset(struct mxt_data *data) > return ret; > > /* Ignore CHG line for 100ms after reset */ > - msleep(100); > + msleep(MXT_RESET_INVALID_CHG); > > mxt_acquire_irq(data); > > @@ -3167,20 +3169,14 @@ static int mxt_probe(struct i2c_client *client, const struct i2c_device_id *id) > return error; > } > > + disable_irq(client->irq); > + > if (data->reset_gpio) { > - data->in_bootloader = true; > - msleep(MXT_RESET_TIME); > - reinit_completion(&data->bl_completion); > + msleep(MXT_RESET_GPIO_TIME); > gpiod_set_value(data->reset_gpio, 1); > - error = mxt_wait_for_completion(data, &data->bl_completion, > - MXT_RESET_TIMEOUT); > - if (error) > - return error; > - data->in_bootloader = false; > + msleep(MXT_RESET_INVALID_CHG); > } > > - disable_irq(client->irq); > - > error = mxt_initialize(data); > if (error) > return error; > -- > 2.17.0 >
diff --git a/drivers/input/touchscreen/atmel_mxt_ts.c b/drivers/input/touchscreen/atmel_mxt_ts.c index 5d9699fe1b55..f97fbb0af020 100644 --- a/drivers/input/touchscreen/atmel_mxt_ts.c +++ b/drivers/input/touchscreen/atmel_mxt_ts.c @@ -194,6 +194,8 @@ enum t100_type { /* Delay times */ #define MXT_BACKUP_TIME 50 /* msec */ +#define MXT_RESET_GPIO_TIME 20 /* msec */ +#define MXT_RESET_INVALID_CHG 100 /* msec */ #define MXT_RESET_TIME 200 /* msec */ #define MXT_RESET_TIMEOUT 3000 /* msec */ #define MXT_CRC_TIMEOUT 1000 /* msec */ @@ -1206,7 +1208,7 @@ static int mxt_soft_reset(struct mxt_data *data) return ret; /* Ignore CHG line for 100ms after reset */ - msleep(100); + msleep(MXT_RESET_INVALID_CHG); mxt_acquire_irq(data); @@ -3167,20 +3169,14 @@ static int mxt_probe(struct i2c_client *client, const struct i2c_device_id *id) return error; } + disable_irq(client->irq); + if (data->reset_gpio) { - data->in_bootloader = true; - msleep(MXT_RESET_TIME); - reinit_completion(&data->bl_completion); + msleep(MXT_RESET_GPIO_TIME); gpiod_set_value(data->reset_gpio, 1); - error = mxt_wait_for_completion(data, &data->bl_completion, - MXT_RESET_TIMEOUT); - if (error) - return error; - data->in_bootloader = false; + msleep(MXT_RESET_INVALID_CHG); } - disable_irq(client->irq); - error = mxt_initialize(data); if (error) return error;
The current reset-gpio support triggers an interrupt storm on platforms using the maxtouch with level based interrupt. The Motorola Droid 4, which I used for some of the tests is not affected, since it uses a edge based interrupt. This change avoids the interrupt storm by enabling the device while its interrupt is disabled. Afterwards we wait 100ms. This is important for two reasons: The device is unresponsive for some time (~22ms for mxt224E) and the CHG (interrupt) line is not working properly for 100ms. We don't need to wait for any following interrupts, since the following mxt_initialize() checks for bootloader mode anyways. This fixes a boot issue on GE PPD (watchdog kills device due to interrupt storm) and does not cause regression on Motorola Droid 4. Fixes: f657b00df22e ("Input: atmel_mxt_ts - add support for reset line") Signed-off-by: Sebastian Reichel <sebastian.reichel@collabora.co.uk> --- Changes since PATCHv2: * fix patch description * use same timeout value for soft and gpio-reset --- drivers/input/touchscreen/atmel_mxt_ts.c | 18 +++++++----------- 1 file changed, 7 insertions(+), 11 deletions(-)