diff mbox series

[v2] arm64: dts: rockchip: Correct GPIO polarity on brcm BT nodes

Message ID 20241018145053.11928-2-didi.debian@cknow.org (mailing list archive)
State New
Headers show
Series [v2] arm64: dts: rockchip: Correct GPIO polarity on brcm BT nodes | expand

Commit Message

Diederik de Haas Oct. 18, 2024, 2:45 p.m. UTC
Paragraph "3.4 Power up Timing Sequence" of the AzureWave-CM256SM
datasheet mentions the following about the BT_REG_ON pin, which is
connected to GPIO0_C4_d:

  When this pin is low and WL_REG_ON is high,
  the BT section is in reset.

Therefor set that pin to GPIO_ACTIVE_HIGH so that it can be pulled low
for a reset.
If set to GPIO_ACTIVE_LOW, the following errors are observed:

  Bluetooth: hci0: command 0x0c03 tx timeout
  Bluetooth: hci0: BCM: Reset failed (-110)

So fix the GPIO polarity by setting it to ACTIVE_HIGH.
This also matches what other devices with the same BT device have.

Fixes: a3a625086192 ("arm64: dts: rockchip: Fix reset-gpios property on brcm BT nodes")
Signed-off-by: Diederik de Haas <didi.debian@cknow.org>
---
Changes in v2:
- Better commit description with references to the datasheet
- Dropped the (self-)blame as it's not useful to evaluate the usefulness
  of this patch

 arch/arm64/boot/dts/rockchip/rk3566-pinenote.dtsi  | 2 +-
 arch/arm64/boot/dts/rockchip/rk3566-radxa-cm3.dtsi | 2 +-
 2 files changed, 2 insertions(+), 2 deletions(-)

Comments

Heiko Stübner Oct. 21, 2024, 3:44 p.m. UTC | #1
On Fri, 18 Oct 2024 16:45:50 +0200, Diederik de Haas wrote:
> Paragraph "3.4 Power up Timing Sequence" of the AzureWave-CM256SM
> datasheet mentions the following about the BT_REG_ON pin, which is
> connected to GPIO0_C4_d:
> 
>   When this pin is low and WL_REG_ON is high,
>   the BT section is in reset.
> 
> [...]

Applied, thanks!

[1/1] arm64: dts: rockchip: Correct GPIO polarity on brcm BT nodes
      commit: 273070dad96f046e622173b595e4719b82188376

Best regards,
Dragan Simic Oct. 23, 2024, 2:28 a.m. UTC | #2
Hello Diederik,

On 2024-10-18 16:45, Diederik de Haas wrote:
> Paragraph "3.4 Power up Timing Sequence" of the AzureWave-CM256SM
> datasheet mentions the following about the BT_REG_ON pin, which is
> connected to GPIO0_C4_d:
> 
>   When this pin is low and WL_REG_ON is high,
>   the BT section is in reset.
> 
> Therefor set that pin to GPIO_ACTIVE_HIGH so that it can be pulled low
> for a reset.
> If set to GPIO_ACTIVE_LOW, the following errors are observed:
> 
>   Bluetooth: hci0: command 0x0c03 tx timeout
>   Bluetooth: hci0: BCM: Reset failed (-110)
> 
> So fix the GPIO polarity by setting it to ACTIVE_HIGH.
> This also matches what other devices with the same BT device have.
> 
> Fixes: a3a625086192 ("arm64: dts: rockchip: Fix reset-gpios property
> on brcm BT nodes")
> Signed-off-by: Diederik de Haas <didi.debian@cknow.org>

I'm a bit late to the party, :) but just wanted to confirm that
the information provided in the patch description is correct.

> ---
> Changes in v2:
> - Better commit description with references to the datasheet
> - Dropped the (self-)blame as it's not useful to evaluate the 
> usefulness
>   of this patch
> 
>  arch/arm64/boot/dts/rockchip/rk3566-pinenote.dtsi  | 2 +-
>  arch/arm64/boot/dts/rockchip/rk3566-radxa-cm3.dtsi | 2 +-
>  2 files changed, 2 insertions(+), 2 deletions(-)
> 
> diff --git a/arch/arm64/boot/dts/rockchip/rk3566-pinenote.dtsi
> b/arch/arm64/boot/dts/rockchip/rk3566-pinenote.dtsi
> index a477bd992b40..0131f2cdd312 100644
> --- a/arch/arm64/boot/dts/rockchip/rk3566-pinenote.dtsi
> +++ b/arch/arm64/boot/dts/rockchip/rk3566-pinenote.dtsi
> @@ -688,7 +688,7 @@ bluetooth {
>  		host-wakeup-gpios = <&gpio0 RK_PC3 GPIO_ACTIVE_HIGH>;
>  		pinctrl-0 = <&bt_enable_h>, <&bt_host_wake_l>, <&bt_wake_h>;
>  		pinctrl-names = "default";
> -		shutdown-gpios = <&gpio0 RK_PC4 GPIO_ACTIVE_LOW>;
> +		shutdown-gpios = <&gpio0 RK_PC4 GPIO_ACTIVE_HIGH>;
>  		vbat-supply = <&vcc_wl>;
>  		vddio-supply = <&vcca_1v8_pmu>;
>  	};
> diff --git a/arch/arm64/boot/dts/rockchip/rk3566-radxa-cm3.dtsi
> b/arch/arm64/boot/dts/rockchip/rk3566-radxa-cm3.dtsi
> index e9fa9bee995a..1e36f73840da 100644
> --- a/arch/arm64/boot/dts/rockchip/rk3566-radxa-cm3.dtsi
> +++ b/arch/arm64/boot/dts/rockchip/rk3566-radxa-cm3.dtsi
> @@ -404,7 +404,7 @@ bluetooth {
>  		host-wakeup-gpios = <&gpio2 RK_PB1 GPIO_ACTIVE_HIGH>;
>  		pinctrl-names = "default";
>  		pinctrl-0 = <&bt_host_wake_h &bt_reg_on_h &bt_wake_host_h>;
> -		shutdown-gpios = <&gpio2 RK_PC0 GPIO_ACTIVE_LOW>;
> +		shutdown-gpios = <&gpio2 RK_PC0 GPIO_ACTIVE_HIGH>;
>  		vbat-supply = <&vcc_3v3>;
>  		vddio-supply = <&vcc_1v8>;
>  	};
diff mbox series

Patch

diff --git a/arch/arm64/boot/dts/rockchip/rk3566-pinenote.dtsi b/arch/arm64/boot/dts/rockchip/rk3566-pinenote.dtsi
index a477bd992b40..0131f2cdd312 100644
--- a/arch/arm64/boot/dts/rockchip/rk3566-pinenote.dtsi
+++ b/arch/arm64/boot/dts/rockchip/rk3566-pinenote.dtsi
@@ -688,7 +688,7 @@  bluetooth {
 		host-wakeup-gpios = <&gpio0 RK_PC3 GPIO_ACTIVE_HIGH>;
 		pinctrl-0 = <&bt_enable_h>, <&bt_host_wake_l>, <&bt_wake_h>;
 		pinctrl-names = "default";
-		shutdown-gpios = <&gpio0 RK_PC4 GPIO_ACTIVE_LOW>;
+		shutdown-gpios = <&gpio0 RK_PC4 GPIO_ACTIVE_HIGH>;
 		vbat-supply = <&vcc_wl>;
 		vddio-supply = <&vcca_1v8_pmu>;
 	};
diff --git a/arch/arm64/boot/dts/rockchip/rk3566-radxa-cm3.dtsi b/arch/arm64/boot/dts/rockchip/rk3566-radxa-cm3.dtsi
index e9fa9bee995a..1e36f73840da 100644
--- a/arch/arm64/boot/dts/rockchip/rk3566-radxa-cm3.dtsi
+++ b/arch/arm64/boot/dts/rockchip/rk3566-radxa-cm3.dtsi
@@ -404,7 +404,7 @@  bluetooth {
 		host-wakeup-gpios = <&gpio2 RK_PB1 GPIO_ACTIVE_HIGH>;
 		pinctrl-names = "default";
 		pinctrl-0 = <&bt_host_wake_h &bt_reg_on_h &bt_wake_host_h>;
-		shutdown-gpios = <&gpio2 RK_PC0 GPIO_ACTIVE_LOW>;
+		shutdown-gpios = <&gpio2 RK_PC0 GPIO_ACTIVE_HIGH>;
 		vbat-supply = <&vcc_3v3>;
 		vddio-supply = <&vcc_1v8>;
 	};